34/10-33 B
Eksport: PDF
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Generell informasjon
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Brønnhistorie
GeneralWell 34/10-33 B is a sidetrack from the vertical appraisal well 34/10-33 on the Gullfaks South structure. It was the first horizontal well ever drilled on the Norwegian continental shelf. The main purpose of the well was to perform a long period test from a horizontal well through the upper part of the Brent Group. The well should provide important production data and the results from the well should be used to calibrate the simulation model for the reservoir and also to update the geological model for this part of the Brent Group.Operations and resultsAppraisal well was sidetracked 27 April 1989 from the vertical at 1840 m, just below the 13 3/8" casing shoe. The well was drilled with the semi-submersible installation Deepsea Bergen to TD at 3942 m in the Late Jurassic Heather Formation. The well bore was drilled with gel/lignosulphonate mud from kick-off to 1864 m and with Interdrill NT oil based mud from 1864 m to TD. The hole was approximately horizontal in the interval 3670 - 3942 m. During setting of the 7" liner for testing of the hydrocarbon zone, the pipe got stuck and broke between the extension pipe and drill string. Fishing was unsuccessful, and the planned test was therefore not possible. Plugging was performed, and Statoil informed NPD and the partners about the alternatives for future operations. After evaluation of FMT data, it was decided to go for a new sidetrack, 34/10-33 C.The formation tops came in close to the prognosis. The Brent Group, top Tarbert Formation was encountered at 3215 m. Sandstones of the Brent Group contained oil and gas. Due to lateral pressure barriers the Tarbert Formation proved to be water bearing in the horizontal part of the well bore, although good oil shows were described on cores and well site samples up to 3816 m.Three cores were cut in the intervals 3742 - 3751 m, 3785 - 3790 m, and 3850.5 - 3860 m in the Tarbert Formation. Two runs with the FMT tool on drill string was performed in the horizontal part of the well. In addition, five tests behind the 9 5/8" casing was performed with CHFT (Cased Hole Formation Tester). One segregated fluid sample was taken with FMT at 3892 m (1 litre water and 8 litres oil/filtrate). Two segregated fluid samples were taken with CHFT at 3299.5 m (3.2 Sm3 gas, 0.9 litre fluid) and at 3335.0 m (2.4 Sm3 gas and 1.1 litre fluid).The well was plugged back and abandoned on 10 July 1989 for the sidetrack 34/10-33 C.TestingNo drill stem test was performed. -
Borekaks i Sokkeldirektoratet
Borekaks i Sokkeldirektoratet Borekaks tilgjengelig for prøvetaking?YESBorekaks i Sokkeldirektoratet Borekaksprøve, topp dybde [m]Borekaksprøve, bunn dybde [m]1850.003942.00 -
Borekjerner i Sokkeldirektoratet
Borekjerner i Sokkeldirektoratet Kjerneprøve nummerKjerneprøve - topp dybdeKjerneprøve - bunn dybdeKjerneprøve dybde - enhet13742.03751.0[m ]23785.03790.6[m ]33850.03859.8[m ]Borekjerner i Sokkeldirektoratet Total kjerneprøve lengde [m]24.4Borekjerner i Sokkeldirektoratet Kjerner tilgjengelig for prøvetaking?YES -
Kjernebilder
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Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet1579639741029113912471513156216101821182118972048204823403008300830123012304532153215335336793897 -
Geokjemisk informasjon
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Dokumenter – eldre Sokkeldirektoratets WDSS rapporter og andre relaterte dokumenter
Dokumenter – eldre Sokkeldirektoratets WDSS rapporter og andre relaterte dokumenter Dokument navnDokument formatDokumentstørrelse [MB]pdf0.21pdf0.17 -
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk)
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk) Dokument navnDokument formatDokumentstørrelse [MB]pdf1.53pdf36.21pdf32.19 -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]4 ARM CAL GR18223419ACBL VDL CCL GR18003475CDL CN GR31853475CHFT HP GR32380CHFT HP GR32990CHFT HP GR33350CHFT HP GR33360CHFT HP GR33580FMT HP GR35513894FMT HP GR35513892GYRO CCL GR16903440MWD - GR RES NEU POR DEN18403942 -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30219.036220.00.00LOTINTERM.20459.026461.01.43LOTINTERM.13 3/81822.017 1/21838.01.53LOTINTERM.9 5/83484.012 1/43493.01.70LOTOPEN HOLE3942.08 1/23942.00.00LOT -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling18401.4421.09.0WATER BASED09.05.198918641.4518.05.5OIL BASED09.05.198921001.4524.03.0WATER BASED03.05.198929821.5824.06.5OIL BASED19.05.198930241.5826.06.0OIL BASED19.05.198930881.5822.07.0OIL BASED19.05.198931711.5825.07.0OIL BASED19.05.198932001.5823.06.5OIL BASED19.05.198932411.5822.06.5OIL BASED19.05.198932411.5826.07.0OIL BASED19.05.198934021.5827.013.0OIL BASED24.05.198934151.5827.06.5OIL BASED24.05.198934581.5827.07.0OIL BASED24.05.198934841.5025.06.5OIL BASED07.06.198934851.5024.06.0OIL BASED08.06.198934931.5828.07.0OIL BASED25.05.198934931.5931.07.0OIL BASED29.05.198934931.4220.06.0OIL BASED02.06.198934961.4218.08.5OIL BASED05.06.198935881.4220.06.5OIL BASED05.06.198936251.4225.07.0OIL BASED05.06.198936281.5324.09.5OIL BASED09.06.198937301.5524.09.0OIL BASED12.06.198938601.5720.010.0OIL BASED19.06.198939421.6028.010.0OIL BASED20.06.1989 -
Trykkplott
Trykkplott Porertrykksdataene kommer fra logging i brønnen hvis ingen annen kilde er oppgitt. I noen brønner der trykk ikke er logget, er det brukt informasjon fra formasjonstester eller brønnspark. Trykkdataene er rapportert inn til Oljedirektoratet og videre prosessert og kvalitetssikret av IHS Markit.Trykkplott Dokument navnDokument formatDokumentstørrelse [MB]pdf0.22