2/5-11
Eksport: PDF
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Generell informasjon
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Brønnhistorie
GeneralWell 2/5-11 was drilled primarily to explore the Sørimne prospect located in the southwestern part of PL 067, which is north of the existing Tor field. The prospect was a stratigraphic chalk play thought to be separate from the hydrocarbon-bearing formation in the nearby well 2/5-7. The main purpose for drilling the well 2/5-11 was to test the hydrocarbon potential within the Maastrichtian Tor formation. A secondary target was to test the hydrocarbon potential in the Ekofisk Formation Tjatse prospect.Operations and resultsThe 2/5-11 well was spudded on 6 September 1997. "Transocean Nordic", a Jack-Up Rig, was used to drill and abandon the well. Operations took 20 days longer than planned. Main reasons for the extended time were 2 days of unplanned coring and 9 days waiting on weather. The well was drilled to a total depth of 3550 m in the Tor formation in the chalk. High viscosity bentonite mud was used to 780 m. From 780 m to TD the well was drilled water based with various combinations of KCl, polymer, PAC, and glycol.
The expected reservoir was encountered at 3362 m, 2 m deeper than prognosed. A FMT fluid sample containing mainly mud filtrate, some gas and small amounts of floating scummy oil was taken at 3444.3 m. An extensive logging program was employed to evaluate the Chalk sequence. After logging was completed, the logging information indicated that hydrocarbons were present and down hole testing was performed. Testing the well in two zones showed that, although hydrocarbons were present, there was a high content of water. Four cores were cut, one in the Ekofisk Formation (3312 m - 3330 m), one across the Ekofisk - Tor boundary (3330 m - 3366 m), and two in the Tor Formation (3393 m - 3419 m and 3418 m - 3465 m). The well was permanently plugged and abandoned as an oil discovery.TestingTwo tests were performed in the well. Test 1 in interval 3363 - 3381 m in the Tor Formation produced a total of 3.8 Sm3 of 38.7 API gravity oil with a Bottom Sediments and Water percentage (BSW) close to 94%. Test 2 in interval 3289 - 3329 m in the Ekofisk Formation involved an acid job to improve recovery. Before the acid job the test produced a total of 12.8 Sm3 of 38.7& API gravity oil with a BSW of 45%. After the acid job the test produced a total of 92 Sm3 oil of 37.1 API gravity with a BSW close to 90%. -
Borekaks i Sokkeldirektoratet
Borekaks i Sokkeldirektoratet Borekaks tilgjengelig for prøvetaking?YESBorekaks i Sokkeldirektoratet Borekaksprøve, topp dybde [m]Borekaksprøve, bunn dybde [m]290.003550.00 -
Borekjerner i Sokkeldirektoratet
Borekjerner i Sokkeldirektoratet Kjerneprøve nummerKjerneprøve - topp dybdeKjerneprøve - bunn dybdeKjerneprøve dybde - enhet13312.03330.0[m ]23330.03366.0[m ]33393.03418.0[m ]43419.03465.0[m ]Borekjerner i Sokkeldirektoratet Total kjerneprøve lengde [m]125.0Borekjerner i Sokkeldirektoratet Kjerner tilgjengelig for prøvetaking?YES -
Kjernebilder
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Palynologiske preparater i Sokkeldirektoratet
Palynologiske preparater i Sokkeldirektoratet Prøve dybdeDybde enhetPrøve typeLaboratorie3000.0[m]DCRRI3010.0[m]DCRRI3020.0[m]DCRRI3030.0[m]DCRRI3040.0[m]DCRRI3050.0[m]DCRRI3060.0[m]DCRRI3070.0[m]DCRRI3080.0[m]DCRRI3090.0[m]DCRRI3100.0[m]DCRRI3110.0[m]DCRRI3120.0[m]DCRRI3130.0[m]DCRRI3140.0[m]DCRRI3150.0[m]DCRRI3160.0[m]DCRRI3170.0[m]DCRRI3180.0[m]DCRRI3190.0[m]DCRRI3200.0[m]DCRRI -
Oljeprøver i Sokkeldirektoratet
Oljeprøver i Sokkeldirektoratet Test typeFlaske nummerTopp dyp
MD [m]Bunn dyp
MD [m]Væske typeTest tidspunktPrøver tilgjengeligDSTDST13381.003363.0028.10.1997 - 21:45YESDSTDST20.000.0003.11.1997 - 01:30YES -
Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet104175230763076308630963181320332033362 -
Spleisede logger
Spleisede logger Dokument navnDokument formatDokumentstørrelse [MB]pdf0.27 -
Geokjemisk informasjon
Geokjemisk informasjon Dokument navnDokument formatDokumentstørrelse [MB]pdf0.60 -
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk)
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk) Dokument navnDokument formatDokumentstørrelse [MB]pdf112.06 -
Borestrengtester (DST)
Borestrengtester (DST) Test nummerFra dybde MD
[m]Til dybde MD
[m]Reduksjonsventil størrelse
[mm]1.03381336319.02.03329328918.1Borestrengtester (DST) Test nummerEndelig avstengningstrykk
[MPa]Endelig strømningstrykk
[MPa]Bunnhullstrykk
[MPa]Borehullstemperatur
[°C]1.046.2401312.047.200129Borestrengtester (DST) Test nummerOlje produksjon
[Sm3/dag]Gass produksjon
[Sm3/dag]Oljetetthet
[g/cm3]Gasstyngde rel. luftGOR
[m3/m3]1.040.8292.0120.800120 -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]DLL MLL MAC CAL GR32153547FMT GR00LWD DPR2073550SBT GR CCL30553493STAR ORIT DGR32203535VSP CST00ZDL CN DPIL HDIL SL32153529 -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30207.036208.00.00LOTSURF.COND.20770.026772.00.00LOTINTERM.13 3/82013.017 1/22020.00.00LOTINTERM.9 5/83220.012 1/43225.00.00LOTLINER73550.08 1/23550.00.00LOT -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling2201.2014.0GEL/DW2301.038.0SW/GEL2541.036.0SW/GEL2831.0310.0DW/GEL5521.186.0DW PHB7751.3037.0KCL/POLYMER7751.135.0SW-GEL12431.3922.0KCL/POLYMER20201.5532.0KCL/SW20201.5532.0KCL/POLYMER21681.6438.0KCL/PAC/GLYCOL25501.6849.0KCL/PAC/GLYCOL27911.7050.0KCL/PAC/GLYCOL29991.6849.0KCL/PAC/GLYCOL29991.5129.0PAC-GLYCOL31201.7048.0KCL/PAC/GLYCOL31951.5028.0PAC/GLYCOL32251.7043.0KCL/PAC/GLYCOL32291.6057.0FW/PAC/GLYCOL32481.5748.0FW/PAC/GLYCOL33301.5530.0PAC33561.5428.0PAC POLYMER33561.5028.0PAC/GLYCOL33601.5429.0PAC-GLYCOL33861.5529.0PAC35501.5433.0PAC35501.5229.0PAC-GLYCOL35561.5430.0PAC POLYMER -
Trykkplott
Trykkplott Porertrykksdataene kommer fra logging i brønnen hvis ingen annen kilde er oppgitt. I noen brønner der trykk ikke er logget, er det brukt informasjon fra formasjonstester eller brønnspark. Trykkdataene er rapportert inn til Oljedirektoratet og videre prosessert og kvalitetssikret av IHS Markit.Trykkplott Dokument navnDokument formatDokumentstørrelse [MB]pdf0.22