6305/1-1
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General information
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Wellbore history
GeneralWell 6305/1-1 is located in the northern part of the Ormen Lange Dome and was the third well drilled on the Ormen Lange Structure, following the two successful wells 6305/5-1 drilled by Hydro in 1997 and 6305/7-1 drilled by BP in 1998. The Egga sand in the Tang Formation was the main target for the well. The sand was predicted to contain gas. The Tare and Lysing Formations were considered as secondary and third target levels, respectively.Operations and resultsWildcat well 6305/1-1 was spudded in a water depth of 863 m on 18 August 1998 with the semi-submersible installation "Transocean Leader" and drilled to a total depth of 4565 m (4551 m TVD) in Late Cretaceous sediments of the Lysing Formation. Well 6305/1-1 was drilled to 2560 m where hole problems made it necessary to plug the well back and perform a technical, sidetrack from 2467 m. The well was drilled with spud mud down to 1610 m and with "Aquacol" KCl/Polymer mud from 1610 to TD. The Egga Member of the Tang Formation and thin sandstones in the Springar Formation were proven in cores from 2558-2623,5 m. Egga sand was encountered even though the reservoir quality was poorer than prognosed. No moveable hydrocarbons were encountered in well 6305/1-1, but weak residual shows were reported in almost the entire Cretaceous section. The Egga sand in well 6305/1-1 proved to be over pressured compared to wells 6305/5-1 and 6305/7-1. Even though some sand was reported from the mud geologist at the predicted intra Tare level this was not considered as a reservoir sand. At Lysing level some thin sandstone layers were encountered, but not considered as a reservoir. Five cores were cut in the well. Four were cut in the Tang and Springar Formations in the interval 2556 m to 2628 m. Recovery for these varied from 10 % to 95 %. The fifth core was cut in the upper part of the Lysing Formation in the interval 3646 m to 3670.5 m. Recovery for this core was 97 %. An MDT fluid sample was taken at 2567.7 m. It contained formation water. The well was permanently plugged and abandoned as a dry well on 19 November 1998.TestingNo drill stem test was performed -
Cuttings at the Norwegian Offshore Directorate
Cuttings at the Norwegian Offshore Directorate Cuttings available for sampling?YESCuttings at the Norwegian Offshore Directorate Cutting sample, top depth [m]Cutting samples, bottom depth [m]1620.004555.00 -
Cores at the Norwegian Offshore Directorate
Cores at the Norwegian Offshore Directorate Core sample numberCore sample - top depthCore sample - bottom depthCore sample depth - uom12556.02573.2[m ]22574.02582.2[m ]32601.02601.9[m ]42610.02623.2[m ]53643.03669.6[m ]Cores at the Norwegian Offshore Directorate Total core sample length [m]66.0Cores at the Norwegian Offshore Directorate Cores available for sampling?YES -
Core photos
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Palynological slides at the Norwegian Offshore Directorate
Palynological slides at the Norwegian Offshore Directorate Sample depthDepth unitSample typeLaboratory1630.0[m]DCRRI1649.0[m]SWCRRI1660.0[m]DCRRI1667.5[m]SWCRRI1690.0[m]DCRRI1715.0[m]SWCRRI1720.0[m]DCRRI1730.0[m]DCRRI1739.0[m]SWCRRI1753.0[m]SWCRRI1778.0[m]SWCRRI1793.0[m]SWCRRI1813.0[m]SWCRRI1850.0[m]DCRRI1879.0[m]SWCRRI1880.0[m]DCRRI1912.0[m]SWCRRI1935.0[m]SWCRRI1948.0[m]SWCRRI1956.0[m]SWCRRI1965.0[m]SWCRRI1977.0[m]SWCRRI1990.0[m]DCRRI2008.0[m]SWCRRI2015.0[m]SWCRRI2024.0[m]SWCRRI2053.0[m]SWCRRI2060.0[m]SWCRRI2071.5[m]SWCRRI2078.0[m]SWCRRI2087.0[m]SWCRRI2103.0[m]SWCRRI2112.0[m]SWCRRI2117.0[m]SWCRRI2142.0[m]SWCRRI2149.0[m]SWCRRI2165.0[m]SWCRRI2198.0[m]SWCRRI2208.0[m]SWCRRI2225.0[m]SWCRRI2235.0[m]SWCRRI2470.0[m]DCRRI2500.0[m]DCRRI2525.0[m]DCRRI2535.0[m]DCRRI2540.0[m]DCRRI2542.0[m]DCRRI2545.0[m]DCRRI2547.0[m]DCRRI2552.0[m]DCRRI2650.0[m]DCRRI2675.0[m]DCRRI2690.0[m]DCRRI2705.0[m]DCRRI2715.0[m]DCRRI2725.0[m]DCRRI2730.0[m]DCRRI2770.0[m]DCRRI2820.0[m]DCRRI -
Lithostratigraphy
Lithostratigraphy Top depth [mMD RKB]Lithostrat. unit8638631734174017402172217223552558260626062827304836403640 -
Composite logs
Composite logs Document nameDocument formatDocument size [MB]pdf0.57 -
Documents – reported by the production licence (period for duty of secrecy expired)
Documents – reported by the production licence (period for duty of secrecy expired) Document nameDocument formatDocument size [MB].pdf182.80.pdf6.65 -
Logs
Logs Log typeLog top depth [m]Log bottom depth [m]CMR GR25402645CST GR24324550CST GR AMS16282235DSI FMI CAL19002544FMI HNGS AMS24143011HALS TLD HGNS DSI GPIT AMS8392235HALS TLD HGNS DSI GPIT AMS23504550MDT GR25572864MWD-MPRLITE/DPR8634560VSP18404560 -
Casing and leak–off tests
Casing and leak–off tests Casing typeCasing diam.
[inch]Casing depth
[m]Hole diam.
[inch]Hole depth
[m]LOT/FIT mud eqv.
[g/cm3]Formation test typeCONDUCTOR30942.036942.00.00LOTINTERM.201605.0261605.01.47LOTINTERM.13 3/82414.017 1/22414.01.63LOTINTERM.9 5/83004.012 1/43004.01.68LOTOPEN HOLE4560.08 1/24560.00.00LOT -
Drilling mud
Drilling mud Depth MD [m]Mud weight [g/cm3]Visc. [mPa.s]Yield point [Pa]Mud typeDate measured8891.10WATER BASED9451.10WATER BASED9461.20WATER BASED16001.3818.0WATER BASED16101.20WATER BASED16151.3216.0WATER BASED24150.0015.0WATER BASED24181.3017.0WATER BASED25561.4524.0WATER BASED25611.4217.0WATER BASED26851.4520.0WATER BASED29001.4621.0WATER BASED29501.4824.0WATER BASED30101.5025.0WATER BASED33721.4719.0WATER BASED43131.4722.0WATER BASED44381.4718.0WATER BASED45601.4721.0WATER BASED -
Pressure plots
Pressure plots The pore pressure data is sourced from well logs if no other source is specified. In some wells where pore pressure logs do not exist, information from Drill stem tests and kicks have been used. The data has been reported to the NPD, and further processed and quality controlled by IHS Markit.Pressure plots Document nameDocument formatDocument size [MB]PDF0.27