30/6-3
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General information
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Wellbore history
GeneralWell 30/6-3 was drilled on the Alpha structure situated in the south-western part of block 30/6. The objective of the well was to penetrate sandstones of Middle Jurassic age and to evaluate their possible content of hydrocarbons.Operations and resultsAppraisal well 30/6-3 was spudded with the semi-submersible installation Deepsea Saga on 16 December 1979 and drilled to TD at 2940 m, 56 m into the Statfjord formation. No significant problem was encountered in the operations, but 13.5 days were lost due to bad weather. The well was drilled with spud mud down to 1757 m and with chrome lignosulphonate/bentonite mud from 1757 m to TD.Oil shows were recorded in claystone/siltstone cuttings at 1993 to 2023 m, in siltstone cuttings at 2095 m, and in limestone cuttings from 2253 m to 2296 m and 2317 m to 2350 m. Top Brent Group came in at 2421 m. It consisted of sandstone interbedded with shale and coals with a main reservoir sand from 2480 to 2513 m. Gas/condensate was proven all through the reservoir. The hydrocarbon/water contact could not be defined, but the presence of hydrocarbons down to the base of the reservoir indicated the contact to be located down flank on the structure. The sandstones of Early Jurassic age ("Intra Dunlin Sand" and the Statfjord Group) were water bearing.Four cores were cut in the interval from 2421 to 2458 m. An RFT fluid sample was taken at 2499 m. FIT fluid samples were taken at 2279 m (traces of gas), 2422 m (gas), 2451 m (small amounts of 32.6 deg API oil), and 2463 m (gas).The well was permanently abandoned on 7 March 1980 as a gas/condensate appraisal.TestingTwo drill stem tests were conducted.DST1 tested the interval 2501 to 2511 m and produced 157 Sm3 oil and 495500 Sm3 gas /day through a 44/64" choke. The GOR was 3170 Sm3/Sm3, the oil gravity was 59.3 deg API, and the gas gravity was 0.657 (air = 1). The down hole flowing temperature was 97.8 deg C.DST2 tested the interval 2421 m to 2432 m and produced 88 Sm3 oil and 280300 Sm3 gas /day through 48/64" and 20/64" chokes in parallel. The GOR was the same as in DST1, the oil gravity was 65.0 deg API, and the gas gravity was 0.645 (air = 1). The down hole flowing temperature was 83.9 deg C. -
Cuttings at the Norwegian Offshore Directorate
Cuttings at the Norwegian Offshore Directorate Cuttings available for sampling?YESCuttings at the Norwegian Offshore Directorate Cutting sample, top depth [m]Cutting samples, bottom depth [m]190.002940.00 -
Cores at the Norwegian Offshore Directorate
Cores at the Norwegian Offshore Directorate Core sample numberCore sample - top depthCore sample - bottom depthCore sample depth - uom12421.02430.7[m ]22431.02437.5[m ]32438.52444.0[m ]42444.12456.0[m ]Cores at the Norwegian Offshore Directorate Total core sample length [m]33.5Cores at the Norwegian Offshore Directorate Cores available for sampling?YES -
Oil samples at the Norwegian Offshore Directorate
Oil samples at the Norwegian Offshore Directorate Test typeBottle numberTop depth
MD [m]Bottom depth
MD [m]Fluid typeTest timeSamples availableDSTTEST12476.002486.00CONDENSATE18.02.1980 - 00:00YES -
Lithostratigraphy
Lithostratigraphy Top depth [mMD RKB]Lithostrat. unit1306807519601994199420662101225623532353242125122512268927682884 -
Geochemical information
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Documents – reported by the production licence (period for duty of secrecy expired)
Documents – reported by the production licence (period for duty of secrecy expired) Document nameDocument formatDocument size [MB]pdf17.43 -
Drill stem tests (DST)
Drill stem tests (DST) Test numberFrom depth MD
[m]To depth MD
[m]Choke size
[mm]1.02476248617.52.02396240719.1Drill stem tests (DST) Test numberFinal shut-in pressure
[MPa]Final flow pressure
[MPa]Bottom hole pressure
[MPa]Downhole temperature
[°C]1.02.0Drill stem tests (DST) Test numberOil
[Sm3/day]Gas
[Sm3/day]Oil density
[g/cm3]Gas grav. rel.airGOR
[m3/m3]1.01574960000.7420.65731702.0882800000.7200.6453170 -
Logs
Logs Log typeLog top depth [m]Log bottom depth [m]CBL GR8001739CBL GR12172565CBL VDL GR13402536CCL96879CCL100153CCL8102454CCL23652424CCL23952536CCL24582528CCL24622536CCL24942485DLL MSFL GR21992582FDC CNL GR17552943GEODIP23992526HDT17402943ISF SON GR SP1262941 -
Casing and leak–off tests
Casing and leak–off tests Casing typeCasing diam.
[inch]Casing depth
[m]Hole diam.
[inch]Hole depth
[m]LOT/FIT mud eqv.
[g/cm3]Formation test typeCONDUCTOR30170.036170.00.00LOTSURF.COND.20889.026900.01.73LOTINTERM.13 3/81715.017 1/21732.01.68LOTINTERM.9 5/82545.012 1/42557.02.10LOTLINER72915.08 1/22915.00.00LOT -
Drilling mud
Drilling mud Depth MD [m]Mud weight [g/cm3]Visc. [mPa.s]Yield point [Pa]Mud typeDate measured1691.05waterbased2731.06waterbased6111.08waterbased16311.3033.0waterbased17321.3238.0waterbased20531.5456.0waterbased23001.5560.0waterbased26241.2546.0waterbased -
Pressure plots
Pressure plots The pore pressure data is sourced from well logs if no other source is specified. In some wells where pore pressure logs do not exist, information from Drill stem tests and kicks have been used. The data has been reported to the NPD, and further processed and quality controlled by IHS Markit.Pressure plots Document nameDocument formatDocument size [MB]pdf0.22