15/12-13 B
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Generell informasjon
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Brønnhistorie
GeneralWell 15/12-13 is located ca 0.8 km northwest of the 15/12-12 (Varg South) Discovery well. The primary objective was to appraise this discovery: to define the oil/water contact, measure current reservoir pressure and fluid gradients, confirm reservoir quality and geometry, and confirm geophysical model in terms of depth to top and base reservoir. Potential Kimmeridgian Sandstone immediately above the main Oxfordian reservoir was seen as secondary objective. The well bore 15/12-13 encountered the Oxfordian sandstones (Intra Heather Formation sandstone) 105 m deeper than the prognosed reservoir, and below the OWC. Since the objective of this well was not met well 15/12-13 A was drilled as a geological sidetrack to 15/12-13. Well 15/12-13 was abandoned in the Rogaland Group due to hole instability problems, and it was decided to drill a second sidetrack. This sidetrack had target approximately 350 m to the northwest of 15/12-12.Operations and resultsAppraisal sidetrack well 15/12-13 B was spudded with the semi-submersible installation West Alpha on 17 May 2003. Kick-off was at 1345 m in 15/12-13. It was drilled to TD at 3151 m in the Triassic Sleipner Formation. The well bore was drilled with Sodium silicate (Barasil CX)/KCl/glycol mud.A total of 134 m MD (128 m TVD) of Kimmeridgian to Late Oxfordian reservoir (2958 m to 3092 m MD) was penetrated in well 15/12-13 B. The oil/water contact was established at 3061.3 m (2964 m TVDSS), and the gas/oil contact at 3027.5 m (2931 m TVDSS). The reservoir was found to be pressure depleted, most likely due to production from the Varg Field, and the gas/oil contact had moved downwards from 2912 m TVDSS in well 15/12-12 (drilled in 2001).No conventional core was cut. The MDT tool was run for pressure measurements and fluid sampling. Gas was sampled at 3010 m, 3017 m, 3021 m, and 3024 m. Oil was sampled at 3028.5 m. After completion of the logging program, the well was permanently abandoned on 11 June 2003 as an oil and gas appraisal.TestingNo drill stem test was performed. -
Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet1051048124022772277228523442520275628772877293929512963296330923092 -
Spleisede logger
Spleisede logger Dokument navnDokument formatDokumentstørrelse [MB]pdf0.31 -
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk)
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk) Dokument navnDokument formatDokumentstørrelse [MB].pdf1.38.PDF14.48 -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]CST GR29353120LWD - GR RES BAT13202656LWD - GR RES BAT26562951LWD - GR RES NEU ALD BAT29513151MDT GR ACTS ECRD29603089MDT GR ACTS ECRD30103028VSP GR20003140 -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30165.036171.00.00LOTSURF.COND.13 3/81315.017 1/21320.00.00LOTINTERM.9 5/82920.012 1/42951.01.88LOTOPEN HOLE3151.08 1/23151.00.00LOT -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling12271.5622.0BARASILC-13B14601.5026.0BARASILC-13A19701.5028.0BARASILC-13A24071.5026.0BARASILC-13A26361.5125.0BARASILC-13A26561.5424.0BARASILC-13B -
Trykkplott
Trykkplott Porertrykksdataene kommer fra logging i brønnen hvis ingen annen kilde er oppgitt. I noen brønner der trykk ikke er logget, er det brukt informasjon fra formasjonstester eller brønnspark. Trykkdataene er rapportert inn til Oljedirektoratet og videre prosessert og kvalitetssikret av IHS Markit.Trykkplott Dokument navnDokument formatDokumentstørrelse [MB]pdf0.22