1/9-5
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Generell informasjon
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Brønnhistorie
GeneralWell 1/9-5 was drilled in the Feda Graben in the southern North Sea, in the saddle between the Tommeliten Gamma-structure and the intrusive salt plug forming the Tommeliten Delta structure. The purpose of the well was to appraise the Tommeliten Gamma discovery made by 1/9-4 and to test the hydrocarbon potential and reservoir quality of the Ekofisk and Tor formations.Operations and resultsAppraisal well 1/9-5 was spudded with the jack-up installation Dyvi Beta on 3 October 1978 and drilled to TD at 3450 m in the Late Cretaceous Hod Formation. The pipe got stuck at 3426 m during a clean-up trip. When trying to come loose the hook broke and the drill string dropped in the hole. This event caused material damage and rig shut-down for three days, but nobody was injured. When fishing the drill string it came loose above the jar but the rest of the BHA (approximately 260 m) was left in the hole. The well was drilled with spud mud down to 435 m, with a lime/"Morex" mud system from 435 m to 1377 m, with lime/"Morex"/Drispac mud from 1377 m to 2725 m, and with lignosulphonate/lignite mud from 2725 m to TD. A lot of hole problems occurred in the 17 1/2" and 12 1/4" sections and this was attributed to the lime/"Morex" mud system.The Ekofisk Formation came in at 3207 m and the Tor Formation at 3282 m. No significant hydrocarbon shows were encountered in any section of the well.One core was cut from 3215.5 to 3 233.5 m, proving a dry carbonate section. No wire line fluid samples were taken.The well was permanently abandoned on 16 December 1978 as a dry well.TestingNo drill stem test was performed. -
Borekaks i Sokkeldirektoratet
Borekaks i Sokkeldirektoratet Borekaks tilgjengelig for prøvetaking?YESBorekaks i Sokkeldirektoratet Borekaksprøve, topp dybde [m]Borekaksprøve, bunn dybde [m]180.003450.00 -
Borekjerner i Sokkeldirektoratet
Borekjerner i Sokkeldirektoratet Kjerneprøve nummerKjerneprøve - topp dybdeKjerneprøve - bunn dybdeKjerneprøve dybde - enhet13215.73234.0[m ]Borekjerner i Sokkeldirektoratet Total kjerneprøve lengde [m]18.3Borekjerner i Sokkeldirektoratet Kjerner tilgjengelig for prøvetaking?YES -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30163.036163.00.00LOTSURF.COND.20428.026436.00.00LOTINTERM.13 3/81367.017 1/21379.01.55LOTINTERM.9 5/82715.012 1/22725.01.90LOTOPEN HOLE3450.08 1/23450.01.91LOT -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]CBL100136CBL VDL1002713FDC CNL CAL GR4293450HDT27183448ISF SONIC GR SP1103452 -
Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet1121766298129813013309531923207320732823346 -
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk)
Dokumenter – rapportert av utvinningstillatelsen (frigitt ihht til regelverk) Dokument navnDokument formatDokumentstørrelse [MB]pdf2.37pdf61.54 -
Dokumenter – eldre Sokkeldirektoratets WDSS rapporter og andre relaterte dokumenter
Dokumenter – eldre Sokkeldirektoratets WDSS rapporter og andre relaterte dokumenter Dokument navnDokument formatDokumentstørrelse [MB]pdf0.20pdf0.06 -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling2201.0556.030.0spud mud10901.2342.08.0waterbased14201.5020.031.0waterbased21901.7819.018.0waterbased24501.8024.018.0waterbased33401.6827.015.0waterbased