6406/12-3 S
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Generell informasjon
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Brønnhistorie
GeneralThe 6406/12-3 S, 6406/12-3 A, and 6406/12-3 B wellbores were drilled in concert on the Pil and Bue prospects in the southern end of the Halten Terrace in the Norwegian Sea. The 6406/12-3 S was the first well to be drilled. It was designed to test a seismic data anomaly and a flat spot recognised in the Pil prospect, at Late Jurassic level.Operations and resultsWildcat well 6406/12-3 S was spudded with the semi-submersible installation Transocean Arctic on 21 January 2014 and drilled to TD at 4001 m (3762 m TVD) in the Late Jurassic Melke Formation. A 9 7/8" pilot hole was drilled from 418 to 1246 to check for shallow gas. No shallow gas was seen. Due to deteriorating hole conditions in the 8 1/2" section it was decided to set 7" liner early, at 3839 m, and continue the well as an unplanned 6" hole to TD. Otherwise, no significant problem was encountered in the operations. The well was drilled with seawater and sweeps down to 1246 m and with XP-07 oil based mud from 1246 m to TD.Contrary to prognosis, there were no Rogn Formation sandstones in the well. Instead, the well encountered Intra Melke Formation sandstones at 3514 m (3276.5 m TVD). These sandstones had good to excellent reservoir quality and contained a 227 m TVD gross hydrocarbon column. The hydrocarbons in the reservoir zone consisted of a 93 TVD m thick gas cap overlying a 134 TVD m oil leg in. The GOC is located at 3608 m (3370 m TVD) and the OWC at 3742 m (3504 m TVD). Pressure data indicated a single gas gradient over an oil leg. Below the OWC, the well penetrated a further thick high net to gross reservoir package of Intra Melke sandstones with a continuous water gradient.Five 54 m consecutive cores were cut in the interval 3524 to 3732 m with 100% overall recovery. RCX fluid samples were taken at 3579.1 m (gas), 3620.3 m (oil), 3641.7 m (oil) and 3758.5 m (water).The well was permanently abandoned on 26 April 2014 as an oil and gas discovery.TestingOne Drill Stem Test was conducted from perforations in the interval 3637.3 to 3724.5 m. The test produced oil at a rate of 1017 Sm3/day through a 56/64" choke. The GOR was 160 Sm3/Sm3 and the measured oil density was 0.850g/cm3 (36 °API). -
Borekaks i Sokkeldirektoratet
Borekaks i Sokkeldirektoratet Borekaks tilgjengelig for prøvetaking?YESBorekaks i Sokkeldirektoratet Borekaksprøve, topp dybde [m]Borekaksprøve, bunn dybde [m]1250.003999.00 -
Borekjerner i Sokkeldirektoratet
Borekjerner i Sokkeldirektoratet Kjerneprøve nummerKjerneprøve - topp dybdeKjerneprøve - bunn dybdeKjerneprøve dybde - enhet13524.03578.2[m ]23578.03632.3[m ]33632.33669.3[m ]43669.33724.3[m ]53724.33733.6[m ]Borekjerner i Sokkeldirektoratet Total kjerneprøve lengde [m]209.7Borekjerner i Sokkeldirektoratet Kjerner tilgjengelig for prøvetaking?YES -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30414.736418.00.00SURF.COND.201238.6261246.01.70FITINTERM.13 3/82265.217 1/22271.01.87FITPROD.9 5/83442.412 1/43450.01.98LOTLINER73838.08 1/23839.00.00OPEN HOLE4001.064001.00.00 -
Borestrengtester (DST)
Borestrengtester (DST) Test nummerFra dybde MD
[m]Til dybde MD
[m]Reduksjonsventil størrelse
[mm]1.03637372522.2Borestrengtester (DST) Test nummerEndelig avstengningstrykk
[MPa]Endelig strømningstrykk
[MPa]Bunnhullstrykk
[MPa]Borehullstemperatur
[°C]1.0Borestrengtester (DST) Test nummerOlje produksjon
[Sm3/dag]Gass produksjon
[Sm3/dag]Oljetetthet
[g/cm3]Gasstyngde rel. luftGOR
[m3/m3]1.010170.845160 -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]LWD - GR RES DEN PWD DIR NPOR SO34503839LWD - GR RES PWD DEN POR SON22603450LWD - GR RES PWD DIR1418LWD - GR RES PWD DIR TT38394001MREX35003820MREX38383965PS35173777PS38413900SBT32963425SLAM3483820SLAM38383900SWC34863507VSP11553990 -
Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet3483481091123012301920192020312235223523182573331233123505351435143912 -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling4181.3414.0KCL Polymer displacement mud4541.0518.0High Viscosity Bentonite Mud4601.3414.0KCL Polymer displacement mud4841.0518.0High Viscosity Bentonite Mud9161.3414.0KCL Polymer displacement mud9641.0518.0High Viscosity Bentonite Mud9801.3414.0KCL Polymer displacement mud9851.6353.0Yellow XP-0710501.0518.0High Viscosity Bentonite Mud11801.4930.0Yellow XP-0712461.4629.0YELLOW XP-07 LOW ECD12461.02KCL Polymer displacement mud12461.4629.0YELLOW XP-07 LOW ECD12521.4918.0Yellow XP-0712801.6353.0Yellow XP-0721951.6140.0YELLOW XP-07 LOW ECD23791.6142.0XP O71.6231761.6539.0Yellow XP-0732331.6540.0YELLOW XP-07 LOW ECD34501.7345.0XP O734501.6536.0YELLOW XP-07 LOW ECD35061.7341.0YELLOW XP-07 LOW ECD36321.7340.0XP O737381.6536.0Yellow XP-0737381.34CaBr Brine37651.7341.0XP-0738391.6127.0YELLOW XP-07 LOW ECD38391.7341.0YELLOW XP-07 LOW ECD40011.6130.0Yellow XP-07