6406/12-3 B
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Generell informasjon
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Brønnhistorie
GeneralThe 6406/12-3 S, 6406/12-3 A, and 6406/12-3 B wellbores were drilled in concert on the Pil and Bue prospects in the southern end of the Halten Terrace in the Norwegian Sea. The S and A wells were planned to target the Pil and the Bue prospects, respectively. The first well, 6406/12-3 S tested 1017 Sm3 oil/day with a GOR of 160 Sm3/Sm3 in Intra Melke Formation sandstones. This result led to the decision within the partnership to drill an appraisal of the Pil discovery. The well was designated 6406/12-3 B and was designed to test the Intra Melke Sandstone reservoir encountered along strike from 6406/12-3 S.Operations and resultsAppraisal well 6406/12-3 B was kicked off at 2355 m in well 6406/12-3 S on 2 May 2014. It was drilled with the semi-submersible installation Transocean Arctic to 4315 m in Late Jurassic sediments belonging to the Melke Formation. No significant problem was encountered in the operations. The well was drilled with XP-07 oil based mud from kick-off to TD.At the top of the Jurassic section, the well encountered a different stratigraphy from the 6406/12-3 S well. Immediately below BCU, a 35 m MD Spekk/Rogn/Spekk succession was penetrated. Hydrocarbons were present within these rocks but not moveable. Below the Spekk Formation, at 3761 m (3440 m TVD), the well encountered over 500 m of Intra Melke Formation sandstones. These sands are interpreted to contain similar facies as those encountered in the 6406/12-3 S discovery immediately below the BCU. The Intra Melke sands contained an 82 m oil column in very good to excellent quality reservoir sandstone with an oil-water contact at 3844 m (3522 m TVD), 18 m deeper than in the 6406/12-3 S well. Pressure data confirmed the same oil gradient as in 6406/12-3 S. There was no gas cap. A second hydrocarbon column of 10 m was seen approximately 360 m below the oil water contact.A total of 165 m core was cut and recovered in three cores in the interval 3703 m to 3868 m. The cores captured rocks from the cap rock (Lyr Formation marls), the Spekk and Rogn formations, and the Intra Melke Formation reservoir sandstones. Fluid samples were taken at 3776 m (oil), 3836.5 m (oil), 3892.1 m (water), and 4082.4 m (water).The well was plugged back to the 13 3/8" casing and permanently abandoned on 11 June 2014. It is classified as an oil appraisal well.TestingNo drill stem test was performed. -
Borekaks i Sokkeldirektoratet
Borekaks i Sokkeldirektoratet Borekaks tilgjengelig for prøvetaking?YESBorekaks i Sokkeldirektoratet Borekaksprøve, topp dybde [m]Borekaksprøve, bunn dybde [m]2360.004315.00 -
Borekjerner i Sokkeldirektoratet
Borekjerner i Sokkeldirektoratet Kjerneprøve nummerKjerneprøve - topp dybdeKjerneprøve - bunn dybdeKjerneprøve dybde - enhet13703.03757.3[m ]23757.33814.3[m ]33814.53869.0[m ]Borekjerner i Sokkeldirektoratet Total kjerneprøve lengde [m]165.8Borekjerner i Sokkeldirektoratet Kjerner tilgjengelig for prøvetaking?YES -
Foringsrør og formasjonsstyrketester
Foringsrør og formasjonsstyrketester Type utforingUtforing diam.
[tommer]Utforing dybde
[m]Brønnbane diam.
[tommer]Brønnbane dyp
[m]LOT/FIT slam eqv.
[g/cm3]Type formasjonstestCONDUCTOR30414.736418.00.00SURF.COND.201238.6261246.01.70FITINTERM.13 3/82347.817 1/22355.00.00PROD.9 5/83692.512 1/43700.00.00OPEN HOLE4315.08 1/24315.01.85FIT -
Logger
Logger Type loggTopp dyp for logg [m]Bunn dyp for logg [m]DS MR FLEX34503839GX UX IM34503839MWD - GR RES AP DIR23553700MWD - GR RES NEU DEN SON AP37004315PCOR34503839RCX34503839SBL34503839SLAM DS CNL CZD AAC DIL34503839VSP34503839 -
Litostratigrafi
Litostratigrafi Topp Dyb [mMD RKB]Litostrat. enhet3483481091123012301961196120872332233224492659345234523695372637263728374837614264 -
Boreslam
Boreslam Dybde MD [m]Egenvekt, slam [g/cm3]Viskositet, slam [mPa.s]Flytegrense [Pa]Type slamDato, måling23301.6154.0XP-0725001.6040.0XP-0731211.6143.0XP O736541.6340.0XP O738141.6146.0XP O739401.5837.0XP O740501.5633.0XP O741091.5437.0XP O743151.5435.0XP-07