34/10-6
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General information
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Wellbore history
GeneralWell 34/10-6 was drilled on the northern part of the Delta structure in block 34/10 in the northern North Sea. It was the fifth well drilled on the structure. All four foregoing wells had tested oil in the Brent Group. The primary objective was to test Middle Jurassic Brent Group. Secondary objectives were sandstones of Early Jurassic age.Operations and resultsAppraisal well 34/10-6 was spudded with the semi-submersible installation Borgny Dolphin on 13 November 1979 and drilled to TD at 2362 m. A total of 14.6% of the rig time was lost due to waiting on weather. The other main causes of downtime was technical failure during cementing of the 9 5/8" casing, followed by two squeeze jobs, repair of subsea equipment and lost circulation. The lost circulation was experienced on several occasions when drilling the 8 1/2" hole. The main reason for this was that the 9 5/8" casing (and 13 3/8" casing) were set too high, causing low formation integrity at the casing shoes. The well was drilled with spud mud down to 308 m and with seawater/polymer from 308 m to TD.The Brent Group sandstones were encountered at 2075 m, about 100 m below the OWC established in the previous wells drilled on the Delta structure. The Brent Group was 215 m thick with 145 m net of good reservoir sands (average porosity = 27.8 %). The Brent Group was water bearing. Oil shows were seen from 1580 m to 1632 m in the Balder Formation, and from 1710 m to 1812 m in the Lista Formation and top Shetland Group, otherwise no evidence of hydrocarbons was seen in the well.No conventional cores were cut. The RFT tool was run for pressure points, but no wire line fluid samples were taken.The well was permanently abandoned on 22 January 1980 as a dry well.TestingNo drill stem test was performed. -
Cuttings at the Norwegian Offshore Directorate
Cuttings at the Norwegian Offshore Directorate Cuttings available for sampling?YESCuttings at the Norwegian Offshore Directorate Cutting sample, top depth [m]Cutting samples, bottom depth [m]320.002362.00 -
Palynological slides at the Norwegian Offshore Directorate
Palynological slides at the Norwegian Offshore Directorate Sample depthDepth unitSample typeLaboratory320.0[m]DCRRI520.0[m]DCRRI720.0[m]DCRRI920.0[m]DCRRI1120.0[m]DCRRI1220.0[m]DCRRI1320.0[m]DCRRI1520.0[m]DCRRI1711.0[m]DCRRI1813.0[m]DCRRI1966.0[m]DCRRI1990.0[m]DC1993.0[m]DC2020.0[m]DCRRI2068.0[m]DCRRI2101.0[m]DCRRI -
Oil samples at the Norwegian Offshore Directorate
Oil samples at the Norwegian Offshore Directorate Test typeBottle numberTop depth
MD [m]Bottom depth
MD [m]Fluid typeTest timeSamples availableDST3037.500.0006.04.1991 - 00:00YES -
Lithostratigraphy
Lithostratigraphy Top depth [mMD RKB]Lithostrat. unit24894697510051100115512171317134713821435145515781578163817571757199019951995199720752075210521652197227322902290 -
Geochemical information
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Documents – reported by the production licence (period for duty of secrecy expired)
Documents – reported by the production licence (period for duty of secrecy expired) Document nameDocument formatDocument size [MB]pdf2.71pdf0.81pdf1.47pdf0.33 -
Logs
Logs Log typeLog top depth [m]Log bottom depth [m]CBL5001805CBL VDL14501802CYBERDIP18032361FDC CNL GR CAL18012362FDC GR CAL6231814HDT18022363ISF SON GR SP2222362VELOCITY4752355 -
Casing and leak–off tests
Casing and leak–off tests Casing typeCasing diam.
[inch]Casing depth
[m]Hole diam.
[inch]Hole depth
[m]LOT/FIT mud eqv.
[g/cm3]Formation test typeCONDUCTOR30308.036308.50.00LOTSURF.COND.20650.026665.01.50LOTINTERM.13 3/81558.017 1/21571.01.79LOTINTERM.9 5/81802.012 1/41815.02.03LOTOPEN HOLE2363.08 1/22363.00.00LOT -
Drilling mud
Drilling mud Depth MD [m]Mud weight [g/cm3]Visc. [mPa.s]Yield point [Pa]Mud typeDate measured2831.06waterbased9501.4141.0waterbased16131.5052.0waterbased16701.6552.0waterbased18181.7956.0waterbased21731.7654.0waterbased23381.7756.0waterbased -
Pressure plots
Pressure plots The pore pressure data is sourced from well logs if no other source is specified. In some wells where pore pressure logs do not exist, information from Drill stem tests and kicks have been used. The data has been reported to the NPD, and further processed and quality controlled by IHS Markit.Pressure plots Document nameDocument formatDocument size [MB]pdf0.21