6507/3-14
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General information
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Wellbore history
GeneralWell 6507/3-14 was drilled to test the Black Vulture on the Halten Terrace in the Norwegian Sea. The objective was to test turbiditic sandstones within the Lange Formation.Operations and resultsWildcat well 6507/3-14 was spudded with the semi-submersible installation West Hercules on 28 July 2021. No shallow gas was expected, but minor gas bubbles was observed streaming from conductor cement ports by ROV when running BOP. Streaming gas bubbles from the conductor port and four seabed locations outside conductor continued throughout well operations with a decreasing trend. A well control incident occurred at 1922 m with 3.9 m3 influx comprising water and some gas. The influx zone was sealed off with a 90 m cement plug and 9 5/8" liner run to 1836 m. Drilling commenced to core point at 3266.7 m, and when pulling out the drill pipe got stuck in Lysing Formation sand. After working to free the pipe a long time without success the section was P&A and a sidetrack 6507/3-14 T2 was kicked off from 1774 m. The sidetrack was drilled to final TD at 3418 m in the Early Cretaceous Lyr Formation. The well was drilled with seawater and hi-vis pills down to 1350 m and with Versatec oil-based mud from 1350 m to the sidetrack kick-off at 1774 m. The sidetrack was drilled with Versatec oil-based mud down to 2898 m and with ExploraDrill oil-based MUD from 2898 m to final TD.The intra Lange Formation target sands were encountered at 3266 m. Approximately 24 m of sandstone with moderate reservoir properties was found. The pressure in the Lange sandstones was measured with WFT and were in a similar pressure regime as measured in the 6507/3-13 well, but the targets were penetrated below the OWC. The only hydrocarbon indication in the well was poor shows in these sandstones. The shows are described as "Spotted moderate yellow fair direct Fluorescence, slow blooming blue, white pale cut Fluorescence, fair blue, white residual fluorescens".No cores were cut, and no fluid sample was taken due to dry well.The well was permanently abandoned on 18 September 2021 as a dry well.TestingNo drill stem test was performed. -
Cuttings at the Norwegian Offshore Directorate
Cuttings at the Norwegian Offshore Directorate Cuttings available for sampling?YESCuttings at the Norwegian Offshore Directorate Cutting sample, top depth [m]Cutting samples, bottom depth [m]1360.003265.00 -
Casing and leak–off tests
Casing and leak–off tests Casing typeCasing diam.
[inch]Casing depth
[m]Hole diam.
[inch]Hole depth
[m]LOT/FIT mud eqv.
[g/cm3]Formation test typeCONDUCTOR36448.742448.70.00INTERM.13 3/81343.817 1/21350.01.58FITINTERM.9 5/81836.012 1/41922.01.73FITLINER72798.08 1/22798.01.83FITLINER72897.08 1/22898.01.82FITOPEN HOLE3267.063267.00.00OPEN HOLE3418.063418.00.00 -
Logs
Logs Log typeLog top depth [m]Log bottom depth [m]GR RES DIR -T244928982LWD - GR RES DIR4491922LWD - NBGR GR RES DIR18363267 -
Lithostratigraphy
Lithostratigraphy Top depth [mMD RKB]Lithostrat. unit39939965913581706170618551855192319801980216524752845284528773379 -
Drilling mud
Drilling mud Depth MD [m]Mud weight [g/cm3]Visc. [mPa.s]Yield point [Pa]Mud typeDate measured4501.6033.08.5Exploradrill13141.3928.06.5Versatec15691.6033.08.0Exploradrill17711.5543.08.0Versatec17741.6231.08.5Exploradrill17781.5241.07.0Versatec17821.5538.09.0Versatec18381.5036.08.5Versatec19221.5535.06.5Versatec20771.5439.07.5Versatec23761.5539.08.5Versatec25521.6232.07.5Exploradrill25851.5538.09.0Versatec26051.6033.07.5Exploradrill26401.5538.010.0Versatec29011.6030.07.0Exploradrill30081.6231.07.0Exploradrill32841.6032.09.0Exploradrill34181.6033.08.0Exploradrill